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6 High Performance Candle Filters for the Sugar Factory in Bury St. Edmunds, England

British Sugar invested into the modernization of their juice purification operation at its factory in Southeast England. 6 Putsch® HKF 200 replaced the old, labor intensive Grand-Pont frame filters in second filtration. Through this project, British Sugar was able to increase its filtration capacity to 1200m³ and lower its solid contents from 10 ppm to <2ppm in filtration quality. Furthermore, its maintenance costs were reduced considerably.

A challenge for our design engineers was to carry out the acidification of the filter socks in the vessel. Therefore, these were sealed from the inside with an acid resistant protective coating to prevent corrosion.

The project was carried out within 6 months from order date to the start-up: the filters were set in operation with the customer’s proprietary control system on time for campaign start in 2014. After the optimization of the process parameters by Putsch® process technicians, the system operates trouble free.

Our British customer is very pleased with the performance, operating life, as well as the control possibilities, particularly now that the bothersome changing of filter cloths (10 to 12 units during campaign) with the old installation is no longer necessary. The company would choose Putsch® High Performance Candle Filters again.